Top End Overhaul 3/02 - 3/03
After 141k miles, started noticing
rather sudden onset of white smoke when leaving a stop light after idling
for a few minutes. This is typically a symptom of worn valve stem
seals, an issue that plagues boosted 2JZ engines. Stem seals
are typically replaced at 80k - 120k on the Supras. Decided to
do a top end overhaul and perform some other upgrades at the same time.
Upon further testing, we found
that number 4 cylinder was marginal in holding pressure on a simple
compression check. Max psi on #1 cylinder was around 178psi, which
is totally normal. #4 and #5 were both fairly low with 140psi on #4
and 150psi on #5. The others were in the mid 160 range which is
decent for a 140k mile engine. Since the compression was
ragged and uneven, and smoke was observed only upon initial acceleration
after idling, we surmised that the stem seals were defective. Some
oil traces were found in the head above #4 at the valve stem seal area.
With the head off the vehicle and turned upside down, the #4 cylinder
didn't hold water. As a test of the top end, you can remove a
cylinder head, tip it upside down, put water in it and see where the water
leaks. Sure enough, a leak was indicated on #4. This
basically indicated that the valve seat (not stem seal) was causing the
leakage. The leaky seal could be responsible for damage or
causing the seat to fail, though. The reason for the smoke could
only point to a stem seal, though- the seat would have nothing to do with
oil burning.
A leakdown test was performed while the head was still on the car.
The results of this test indicate that #4 cylinder was leaking at the
exhaust port. The leakdown # was 65/80, Good numbers on a 140k
engine would be 70-75+/80.
With the head exposed but still on the car, we could see some remnants of
dried coolant (see picture) above the 3-4 cylinders. It is unknown
whether this fluid came through the head gasket or leaked down through the
throttle body or some other area. Upon removal of the head,
the gasket areas around the sealing area of the head indicated a small
possible leak, but nothing obvious. This could also contribute to a
low compression situation although a leak down test didn't reveal any
noise through the head gasket into the cooling system.
The head was reconditioned, a 3 angle valve job was performed, and the
head was ported on both sides. It was re-assembled with stiffer
Crower valve springs and a Crower 268/270 regrind of the original cam.
The reground cam also has significantly higher lift. The
regrind of the cam altered the basecircle necessitating lash caps on the
stems themselves. It also required some esoteric shims that
Lexus doesn't normaly stock.
With the head back from the machine shop, a new NA spec headgasket was
installed and the head was re-attached and torqued to the car with stock
head bolts.
With the head back on the car, we re-tested the engine with another leak
down test. This time the test came back with lowest cylinder at
78/80 indicating exceptional sealing. Piston rings, cylinder walls
and pistons themselves were cleaned and deemed to be in very good overall
shape, especially given the mileage.
The re-assembly process proceeded, the stock but ported lower and upper
manifolds were fitted, the slightly ported throttle body was fitted to the
stock fuel rail. An EGR bypass mod was installed, with the EGR
system completely removed from the system. A replacement Aeroquip
oil drain hose was fitted to the lower oil pan to replace a failing one.
It was determined that the original hose was not cut to the proper length,
with the extra slack causing a kink and oil backup resulting in huge
amounts of smoke on some occasions. A word of caution to
Toyomoto kit builders- this hose as supplied is not the correct length.
The kit instructions suggest cutting to a short enough length to avoid
kinks, which was not done.
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